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TOW TANK Having
a test facility like the tow tank already built and right on campus was
an invaluable resource. That being said, there were a few problems with
the system initially. Due to infrequent use and the harsh, damp
"marine" environment of the Aquaculture Research Center, corrosion was
a problem in many places. The rails on which the carriage rides needed
to be sanded smooth to allow the carriage to travel easily. The guards,
which protected bystanders from the rails and the drive cable, had
rusted and migrated in towards the carriage to the point that they
touched the carriage in some places along the track. These rails were
unbolted from there mounts and moved back away from the carriage. Also,
the drive cable had to be realigned on the drive drum to allow the
carriage to travel the full length of the tank.
Tow tank with carriage up on blocks for maintenance Most
importantly, a major design flaw was noticed on the carriage trucks.
The carriage had two trucks on the drive side. Each truck had two
forks, which three wheels each. Two of the wheels were non load bearing
stability wheels, which wrap around the rail. The third wheel was the
load bearing wheel, which was supported by a bolt that was canitlivered
from one side of the fork. The major design flaw was with this bolt.
Even with the carriage unloaded, these bolts were bending enough to
cause the wheel to contact the top of the fork. This made the carriage
movement sporadic. After disassembly of the carriage, it was evident
that the bolts of the load bearing wheels had yielded. Three possible
solutions were conceptualized to solve this problem:
1. Replace the existing bolts with bolts of the same size but made of harder material 2. Replace the existing bolts with bigger bolts that step down to the needed size 3. Add a support block on the unsupported side of the wheel to fully support the bolt 
Solution 1
Solution 2
Solution 3
After analysis, solution three was
decided to be the best. This modification was predicted to raise the
factor of safety of the fork system from less than one to 28. While
solutions one and two would theoretically work, they would only
increase the factor of safety by at most two. The trucks were
removed and a slot was machined into each fork to accept a small
rectangular precision machined aluminum block. This block was threaded to accept the drive
wheel bolt, and was screwed into place on the fork. Installation and
testing of these modified forks showed significant improvement in the
carriages travel characteristics with no yielding of the load bearing
bolts.
Carriage truck forks after modification
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